Waste Water Engineering A sewer running partially full and hurried with back filled, fails in compression due to Superimposed traffic loads Weight of the back fill All listed here Weight of the pipe Superimposed traffic loads Weight of the back fill All listed here Weight of the pipe ANSWER DOWNLOAD EXAMIANS APP
Waste Water Engineering If the depletion of oxygen is found to be 2.5 mg/litre after incubating 2.5 ml of sewage diluted to 250 ml for 5 days at 20°C, B.O.D. of the sewage is 50 mg/l 250 mg/l 100 mg/l 150 mg/l 50 mg/l 250 mg/l 100 mg/l 150 mg/l ANSWER DOWNLOAD EXAMIANS APP
Waste Water Engineering If a 2% solution of sewage sample is incubated for 5 days at 20°C and the dissolved oxygen depletion was found to be 8 mg/l. The BOD of the sewage is 400 mg/l 300 mg/l 200 mg/l 100 mg/l 400 mg/l 300 mg/l 200 mg/l 100 mg/l ANSWER DOWNLOAD EXAMIANS APP
Waste Water Engineering The dimensions of a rectangular settling tank are: length 24 m, width 6 m and depth 3 m. If 2 hour detention period for tanks is recommended, the rate of flow of sewage per hour, is 204 cu.m 212 cu.m 208 cu.m 216 cu.m 204 cu.m 212 cu.m 208 cu.m 216 cu.m ANSWER DOWNLOAD EXAMIANS APP
Waste Water Engineering If the discharge of a sewer running half is 628 1.p.s., i = 0.001, and n = 0.010, the diameter of the sewer, is 1.59 m 1.69 m 1.39 m 1.49 m 1.59 m 1.69 m 1.39 m 1.49 m ANSWER DOWNLOAD EXAMIANS APP
Waste Water Engineering The normal values of over flow rates for sedimentation tanks using coagulant, ranges between 25,000 to 35,000 litres/sqm/day 50,000 to 60,000 litres/sqm/day 80,000 to 100,000 litres/sqm/day 40,000 to 50,000 litres/sqm/day 25,000 to 35,000 litres/sqm/day 50,000 to 60,000 litres/sqm/day 80,000 to 100,000 litres/sqm/day 40,000 to 50,000 litres/sqm/day ANSWER DOWNLOAD EXAMIANS APP